I see quite a few posters have chimed in with questions and comments - I promise I will address them all in short order. But first I wanted to wrap up the cliff-hanger I left off with a couple days ago...
And by cliff-hanger I am of course referring to the test conducted with what can only be adequately characterized as a silly-stupid obscene amount of NT-H1 placed on my 3770k :whiste:
Is that an ear of corn I see in there? D:
(I don't care who ya are, that's funny right there)
After testing, naturally I removed the H100 from the mount and naturally the CPU stuck fast to the H100.
^ this happens with all the TIMs, it is nothing unique to this specific test condition, just thought I'd share the photo.
One thing to note here is that despite the ridiculous amount of NT-H1 I added, it still wasn't enough to cause a bunch of TIM to squeeze out and make a mess of everything. There was enough of a gap between the CPU PCB and the H100 that the NT-H1 was able to basically stay within the confines of the CPU PCB.
^ this is the process I went to using for removing the CPU from the H100 if I wanted to preserve the imprint left in the TIM on the H100 and on the 3770k as best as possible with minimal smearing. It looks like I am training to become a dental hygienist
"open wide please!"
Once I got the CPU off the H100, here's what the imprint on the H100 looked like:
^ We can seen that despite the copious quantity of TIM used the CPU die itself actually made relatively good contact with the H100 as indicated by the visibly detectable areas of exposed copper in the central rectangle area.
And the die itself?
Not bad. Yeah there is crapload of NT-H1 sitting on top of the PCB itself surrounding the die but you can also clearly make out the CPU silicon die sitting in the middle indicating that basically the compression of the H100's mounting pressure did the intended job of ensuring a reasonably good mount was attained.
And the results:
Interestingly the idle temperatures were completely unaffected by the slathered layer of NT-H1.
No big surprise here in that the excessive amount of TIM resulted in elevated temperatures when the CPU is under a load, we all expected this, but I don't think we expected the magnitude per se.
It is surprising to me just how minimal the impact was in terms of thermal performance. At most we are looking at 6°C increase in operating temperatures at the very high end of the OC'ing spectrum of 4.9GHz.
I expected this test to be the epitome of worst-case scenario, that it would be a disastrous setup which would result in operating temperatures that were far worse than those observed with IC Perihelion or TX-1.
Instead what we find is that even under such a worst-case completely silly over-application of NT-H1 the resulting thermal performance only a smidgen worse than the best results obtained with IC Diamond (within a degree or two) and was still better than the best results obtained with TX-2, AS5, MX-4, IC Perihelion and TX-1.
What this goes to show is that at least for this particular setup and application (bare die mounting with an H100), the amount of TIM you use is only of secondary importance to the specific type of TIM you are using.
Start off putting your best foot forward by choosing to use a quality high-performing TIM and at worst you are going to bungle the application and mount and set yourself back by 5-6°C or so.
That may be news to absolutely none of you, I may be the last person on earth to have come to this realization, but even if that is the case I am still happy to have at least caught up to the rest of you and it only cost me a $10 tube of NT-H1 for the education :thumbsup:
And by cliff-hanger I am of course referring to the test conducted with what can only be adequately characterized as a silly-stupid obscene amount of NT-H1 placed on my 3770k :whiste:

(I don't care who ya are, that's funny right there)
After testing, naturally I removed the H100 from the mount and naturally the CPU stuck fast to the H100.

^ this happens with all the TIMs, it is nothing unique to this specific test condition, just thought I'd share the photo.
One thing to note here is that despite the ridiculous amount of NT-H1 I added, it still wasn't enough to cause a bunch of TIM to squeeze out and make a mess of everything. There was enough of a gap between the CPU PCB and the H100 that the NT-H1 was able to basically stay within the confines of the CPU PCB.

^ this is the process I went to using for removing the CPU from the H100 if I wanted to preserve the imprint left in the TIM on the H100 and on the 3770k as best as possible with minimal smearing. It looks like I am training to become a dental hygienist
Once I got the CPU off the H100, here's what the imprint on the H100 looked like:

^ We can seen that despite the copious quantity of TIM used the CPU die itself actually made relatively good contact with the H100 as indicated by the visibly detectable areas of exposed copper in the central rectangle area.
And the die itself?

Not bad. Yeah there is crapload of NT-H1 sitting on top of the PCB itself surrounding the die but you can also clearly make out the CPU silicon die sitting in the middle indicating that basically the compression of the H100's mounting pressure did the intended job of ensuring a reasonably good mount was attained.
And the results:

Interestingly the idle temperatures were completely unaffected by the slathered layer of NT-H1.
No big surprise here in that the excessive amount of TIM resulted in elevated temperatures when the CPU is under a load, we all expected this, but I don't think we expected the magnitude per se.
It is surprising to me just how minimal the impact was in terms of thermal performance. At most we are looking at 6°C increase in operating temperatures at the very high end of the OC'ing spectrum of 4.9GHz.
I expected this test to be the epitome of worst-case scenario, that it would be a disastrous setup which would result in operating temperatures that were far worse than those observed with IC Perihelion or TX-1.
Instead what we find is that even under such a worst-case completely silly over-application of NT-H1 the resulting thermal performance only a smidgen worse than the best results obtained with IC Diamond (within a degree or two) and was still better than the best results obtained with TX-2, AS5, MX-4, IC Perihelion and TX-1.
What this goes to show is that at least for this particular setup and application (bare die mounting with an H100), the amount of TIM you use is only of secondary importance to the specific type of TIM you are using.
Start off putting your best foot forward by choosing to use a quality high-performing TIM and at worst you are going to bungle the application and mount and set yourself back by 5-6°C or so.
That may be news to absolutely none of you, I may be the last person on earth to have come to this realization, but even if that is the case I am still happy to have at least caught up to the rest of you and it only cost me a $10 tube of NT-H1 for the education :thumbsup: