I'll stop spilling this info in to other threads. At work now, so I can't collect more data at the moment, and it was late last night when I finished.
This info is with NT-H1 between the die and IHS, IHS shortened to make it more snug against the die, IHS lapped, H100 lapped (though both were lazy lapping jobs), and IX between the IHS and H100. IX installation on my H100 went *nothing* like the instructions. My method was more, Oh crap, it hit 105 and stayed there, now it has blue screened, let me tighten the H100 on down and hope that the stuff melted (it had). On the H100, I have an extra set of the stock washers for the bracket (so 2 thick instead of one). I didn't like that it put a hard limit on how tight it could go because of how loose it originally was.
Here's 1.4V just for grins (LLC wasn't high enough to maintain the voltage under load and I got droop)
Here's what I usually leave it at. IBT didn't get hotter than 65C at this. Interesingly, the P95 and IBT gap appears to have closed (though this is after 45 minutes of P95 too).
grkM3's request:
This info is with NT-H1 between the die and IHS, IHS shortened to make it more snug against the die, IHS lapped, H100 lapped (though both were lazy lapping jobs), and IX between the IHS and H100. IX installation on my H100 went *nothing* like the instructions. My method was more, Oh crap, it hit 105 and stayed there, now it has blue screened, let me tighten the H100 on down and hope that the stuff melted (it had). On the H100, I have an extra set of the stock washers for the bracket (so 2 thick instead of one). I didn't like that it put a hard limit on how tight it could go because of how loose it originally was.
Here's 1.4V just for grins (LLC wasn't high enough to maintain the voltage under load and I got droop)
Here's what I usually leave it at. IBT didn't get hotter than 65C at this. Interesingly, the P95 and IBT gap appears to have closed (though this is after 45 minutes of P95 too).
grkM3's request:
Last edited: