Tested every injector and found 1 dead and two additional out of spec.
So pulled hoses and bolts for 3 hours to pull the plenum off and delete the IACV, EGR, and various vacuum hoses to clean up the engine bay.
Doing timing belts and whatever else I can find wrong this week.
Ordered 6 new style injectors with needed parts retrofit my old style rails to new style. I decided to stay stock flow rate so I can go completely stock and tune later. I want to catch on on the body and small necessary pieces before I decide to go faster. Body work is going to hurt a little. I am budgeting about 1k.
Once I hear it running and out of limp mode I will be very happy. Hopefully by friday!
I have more pictures of the tear down if you guys are interested.
Knuckles definitely took a beating on this one....