- Aug 30, 2000
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After a week of checking out one of our WRXs trying to find a boost leak and/or broken part, it seems the trouble all along was a bad tank of gas causing the ECU to cut boost (7psi max, spring pressure of the wastegate actuator) and some detonation under load.
I should have looked at this possibility first as the simplest explanation is usually right. But, I was fooled because we filled our other WRX at the same station the following day and experience no driveability issues. I guess that's the difference between being modified and stock.
Anyway, since my weak rant is weak, I'll just complain that after filling about 2/3 of a tank with real 91, the car definitely drives better but still isn't hitting full boost and is still pinging a bit. Hopefully another tank of 91 will bring things back to normal.
I should have looked at this possibility first as the simplest explanation is usually right. But, I was fooled because we filled our other WRX at the same station the following day and experience no driveability issues. I guess that's the difference between being modified and stock.
Anyway, since my weak rant is weak, I'll just complain that after filling about 2/3 of a tank with real 91, the car definitely drives better but still isn't hitting full boost and is still pinging a bit. Hopefully another tank of 91 will bring things back to normal.
